Note the gray swirls in the otherwise deep red transmission oil. That's the silicon, from what I understand, of the viscous coupler that is no longer in its enclosed container. That's what happens when it blows. There's an enclosed can inside that has spider gears (as you would expect from a differential) and clutch discs. See this discussion thread at IFSJA.org for a peek inside the VC. That gray goo is what is floating in my transfer case oil. Rather than replace the coupler (which is a $400 part in an irritating, vacuum actuated transfer case that I'd have to rebuild), I'm shopping for something else that will bolt up to the TF727 transmission. I can buy a rebuilt 229 for about seven hundred, but I have had too many issues with the vacuum lines (they've been "fixed" three times by three reputable shops) to want to put money into such a thing. Why pay so much to get back what I already don't like?
Monday, May 6, 2013
Pulled the transfer case, confirmed its death ...
To verify that the NP229 viscous coupler is indeed dead (and by that, I mean cracked open and no longer functional), I drained the fluid. Here's what I found:
Saturday, May 4, 2013
And then the transfer case grenaded ... Ugh
So frustrating. Every time I get something done, I feel like I get a new problem. I love this Jeep, but it's starting to piss me off. As it's at the smog shop, the transfer case starts to crunch. The smog guy had me take him for a ride around the parking lot once the noise kicked in. It sounded like gravel in a coffee can. I don't believe he did anything to kill it. From what I understand, the only way to kill one is to have the locking hubs up front disengaged, and then you shift into four wheel drive. I don't know why he would have done either of those given that his smog test equipment is designed only to work on one set of drive wheels (front or rear). I limped it home and started thinking about my options are. Is it dead? If so, do I rebuild it, do I replace it, or do I upgrade it?
Past smog ... barely
Now that I've got the Howell system installed, I took it to a STAR station to get it approved. I was worried about the new system's legality (not whether it was actually legal but whether the smog dude would know that it's legal). He was an older guy, and I'd taken the carburated version of my rig to him, only to learn that the carb was so out of whack that the NO level was off the charts. I'd affixed the sticker on the passenger side of the front core support near the battery tray, had a copy of the C.A.R.B. executive order certifying the Howell system, and just hoped for the best.
It did indeed pass, but only withthe smog dude "heating the shit out of" the catalytic converter. He says the universal cats are only good for a few tests, every other year, which is precisely how long this one lasted. I'll get a new, better cat next year, maybe.
Monday, April 29, 2013
Sunday, April 14, 2013
Sunday, April 7, 2013
Monday, March 25, 2013
Installing Side steps
I've got wee ones--three--plus a perfect five foot wife. A tall rig causes accessibility issues that have been building for years. I'd looked at getting some rock sliders from BJ'S Off Road, inverted to tuck not quite so high up into the door rockers. I would have loved to have had them, but they were cost prohibitive (not that BJ's overpriced them, just that they were more, with shipping, than I could reasonably afford).
There are no bolt-on steps for these idiosyncratic vehicles, despite their long run from 1963 to 1991. After doing a bit of searching on Amazon, I found a step that I thought might work, so I ordered one (I'd eventually need four, one for each door).
It wasn't a perfect fit, and there were some installation issues that I'll point out below; however, they do the job and look right, so I'm pleased.
They screw into the vertical back of the lower rocker panel (where the open-backed square portion of the bracket is) and then bolt through the rocker seam and up into the bottom of that same square bracket. In the picture below, you can see the silver heads of the bolts.
There are no bolt-on steps for these idiosyncratic vehicles, despite their long run from 1963 to 1991. After doing a bit of searching on Amazon, I found a step that I thought might work, so I ordered one (I'd eventually need four, one for each door).
It wasn't a perfect fit, and there were some installation issues that I'll point out below; however, they do the job and look right, so I'm pleased.
They screw into the vertical back of the lower rocker panel (where the open-backed square portion of the bracket is) and then bolt through the rocker seam and up into the bottom of that same square bracket. In the picture below, you can see the silver heads of the bolts.
The above picture of the step for the driver's side rear door also highlights the primary installation difficulty: the frame rail and front spring perch for the rear leafs. It's a tight fit to get a drill in there to screw a pilot hole and then get the screw itself in there. I had to do it at a steep angle and work hard at it for quite some time to get it in there. It was a real pain. This was the first one I installed, and if I had to do it again, it'd be the second or the third so that I wouldn't have to learn not only how to install the step but also how to do it in the hardest spot. It alone took me as long as the other three. Additionally, note the stamped L-bracket in the upper right corner of the picture that joins the Jeep's flood to the rocker panel. I used that as a point of reference to get both rear door steps aligned in parallel with one another.
Here's the front passenger side step mounted up. This shot shows another bracket that connects the Jeep floor to rocker panel. It also worked nicely as a point of alignment for the two front steps. These were considerably easier to install, though the frame rail on the left was still a bit of a bugaboo.
They aren't aesthetically perfect, sticking out a little more I had expected, but they work well for the kids and wife, which is great..
Saturday, March 9, 2013
Getting the cargo area squared away
I didn't want anything flopping around when the rig is taken off road, so I had to get the spare and the winch more properly secured. A drill, some bolts, and a few little tricks got the job done.
I bought new on eBay the Mile Marker 2" receiver hitch winch mount (P/N 60-06495) that would let me use the recovery tool front or rear, given that I'd had Jeeps R Us weld a receiver hitch to the front frame cross member under the radiator (parts and labor, $450).
All in all, it weighs one hundred plus pounds, so I'm hoping not to have to lug it around much. But I'd rather have that weight in the back of the Jeep over the rear axle than hanging off the front, messing with air flow to the radiator, as well as departure angles. I also didn't have to buy a gigantor bumper and pay to have it shipped, so I'm good with that, too.
To get the winch mount secured in the back of the Jeep, I bought an RV bumper adapter that is designed to hold a spare tire holder that bolts to a 2" receiver mount. To make it work for my purpose, I tossed aside the extra long grade 5 bolts and bought 2" grade 8 bolts from the local home center. The adapter tucks up behind the passenger side of the back seat, away from fuel lines and the gas tank. At an angle, the winch mount slides in under the hi-lift jack to stay secure and out of the way.
While I was working around in the back, I added two eye bolts to hook a tie-down strap to, holding the spare tire to the hi-lift jack. It gives me some free space underneath to put my winch recovery bag, some tools, and a five gallon bucket of spare parts, hoses, etc.
I bought new on eBay the Mile Marker 2" receiver hitch winch mount (P/N 60-06495) that would let me use the recovery tool front or rear, given that I'd had Jeeps R Us weld a receiver hitch to the front frame cross member under the radiator (parts and labor, $450).
All in all, it weighs one hundred plus pounds, so I'm hoping not to have to lug it around much. But I'd rather have that weight in the back of the Jeep over the rear axle than hanging off the front, messing with air flow to the radiator, as well as departure angles. I also didn't have to buy a gigantor bumper and pay to have it shipped, so I'm good with that, too.
To get the winch mount secured in the back of the Jeep, I bought an RV bumper adapter that is designed to hold a spare tire holder that bolts to a 2" receiver mount. To make it work for my purpose, I tossed aside the extra long grade 5 bolts and bought 2" grade 8 bolts from the local home center. The adapter tucks up behind the passenger side of the back seat, away from fuel lines and the gas tank. At an angle, the winch mount slides in under the hi-lift jack to stay secure and out of the way.
While I was working around in the back, I added two eye bolts to hook a tie-down strap to, holding the spare tire to the hi-lift jack. It gives me some free space underneath to put my winch recovery bag, some tools, and a five gallon bucket of spare parts, hoses, etc.
All neat and tidy.
I imagine at some point I'm going to want to get the spare out of the rear cargo area, so when that happens, I'll either upgrade the rear bumper to a custom one with a swing out tire carrier (which would be a thousand bucks shipped) or keep it in the garage when I'm not wheeling (using the stock spare under floor above the rear axle as an emergency "mini" spare), and just throw it up on the roof for wheeling trips.
Friday, December 7, 2012
MSD install goes to hell, and the Jeep goes to the shop
I've been frustrated routinely and repeatedly with the ignition system in these things. All that V8 goodness (in what is considered a pretty good package by AMC, even if it doesn't get the respect it deserves) is stifled too often by weak spark or no spark. The cheap ignition module sucks. The stock distributor cap contact points are a bit too close together, sometimes leading to spark overlap. The ignition modules can burn out (as happened to me when I was hoping to take the family wheeling in Joshua Tree a few years ago). Frustrating.
So one recommendation from the good folks at IFSJA.org was to ditch the stock ignition module and go with a MSD box. I bought one off of Amazon.com, including the adapter plug to get it to mate with my stock distributor. The coil was good, so this seemed like a good idea.
So one recommendation from the good folks at IFSJA.org was to ditch the stock ignition module and go with a MSD box. I bought one off of Amazon.com, including the adapter plug to get it to mate with my stock distributor. The coil was good, so this seemed like a good idea.
What a disaster.
I mounted the box on the driver's side near the charcoal canister and cruise control box. It fit easily and allowed across the engine access to battery, the coil, and the distributor.
Unfortunately, I just can't get the dang thing to run. I've got it hooked up right (I think), and I'm getting spark when I do the bolt-in-the-plug-wire test against the inner fender. But when it is all plugged in and ready to go, I'm getting backfires out the carb. Timing is off.
I bought a timing light, but it's too cheap to be of much use. A waste of money. I tried rotating the distributor a little in each direction, but this made no substantive change. I'm having a hard time figuring out how timing could have jumped so far without the distributor moving. The timing chain is an Edelbrock double roller and has maybe a thousand miles on it. I'm sick of this.
It's been several days. I was worried that maybe it wasn't getting fuel, so I tried to roll it down the hill from its parking spot beside the garage, but that was a disaster too. It got caught up on a damned yucca at first, but eventually I got it in the street down in front of my neighbor Frank's house. He's a good guy and doesn't mind at all. Parked on his driveway is an old Chevy pickup with a camper shell. It gets started up and revved high every few days to get it alive. I'm not sure the hard revving is helping it, especially since it doesn't get driven much, but that's his business.
Now the transmission is leaking an insane amount. What the hell is going on? My Jeep is acting a bit geriatric: has no energy and can't control its bladder.
I'm going to have to give up on this for now. I've called Jeeps R Us in Laguna. They have a great reputation for getting old Jeeps running, even being featured in JP Magazine a few times. There's even a gigantic Cherokee FSJ that they have named Matilda that is a running billboard for their skills. I'm calling a tow truck, dropping this thing off, and throwing money at it (or out the window). They'll get the tranny leak fixed and the starting issue resolved, I'm sure.
----------UPDATE------------
I got the Jeep back in mid-January '13 but forgot to add in a blog entry to mark the date. The work was incredibly expensive, which irritates me for two reasons: 1) I didn't want to spend so much money just to get it running when it already had been; 2) Jeeps R Us was lousy in communicating the cost of the repair work for my approval. I was just confronted with sticker shock when I got the call that the Jeep was ready. The vast majority of the cost was labor alone, and I don't see how trained mechanics should struggle so much just getting a Jeep started when the engine's been rebuilt and the bulk of the ignition system parts were in perfectly fine operating condition (testified to by the fact that they did not need to be replaced). They put in a new rotor for distributor and a new coil and adjusted the timing. Seems like they could have been more efficient and effective with their time (which equals my money). Hell, fixing the tranny leak was only a third of their labor bill.
On the plus side, they welded on a front Class Three receiver hitch using a factory hitch they had lying around the shop. This wasn't expensive, comparatively.
Jeeps R Us got the job done, but I'm not impressed with their billing/estimate process or their communication, so I'll be looking elsewhere for future FSJ repair work.
Now the transmission is leaking an insane amount. What the hell is going on? My Jeep is acting a bit geriatric: has no energy and can't control its bladder.
I'm going to have to give up on this for now. I've called Jeeps R Us in Laguna. They have a great reputation for getting old Jeeps running, even being featured in JP Magazine a few times. There's even a gigantic Cherokee FSJ that they have named Matilda that is a running billboard for their skills. I'm calling a tow truck, dropping this thing off, and throwing money at it (or out the window). They'll get the tranny leak fixed and the starting issue resolved, I'm sure.
----------UPDATE------------
I got the Jeep back in mid-January '13 but forgot to add in a blog entry to mark the date. The work was incredibly expensive, which irritates me for two reasons: 1) I didn't want to spend so much money just to get it running when it already had been; 2) Jeeps R Us was lousy in communicating the cost of the repair work for my approval. I was just confronted with sticker shock when I got the call that the Jeep was ready. The vast majority of the cost was labor alone, and I don't see how trained mechanics should struggle so much just getting a Jeep started when the engine's been rebuilt and the bulk of the ignition system parts were in perfectly fine operating condition (testified to by the fact that they did not need to be replaced). They put in a new rotor for distributor and a new coil and adjusted the timing. Seems like they could have been more efficient and effective with their time (which equals my money). Hell, fixing the tranny leak was only a third of their labor bill.
On the plus side, they welded on a front Class Three receiver hitch using a factory hitch they had lying around the shop. This wasn't expensive, comparatively.
Jeeps R Us got the job done, but I'm not impressed with their billing/estimate process or their communication, so I'll be looking elsewhere for future FSJ repair work.
Friday, July 20, 2012
Emergency Brake Cable
At the new house, my Jeep sits up on the side of the house at the top of a small hill. There's a slight slope to the Jeep's landing pad. I've never quite gotten the emergency brake cable set to how I like it; heck, even the brake shop that I took it to in Redlands couldn't get it adjusted satisfactorily.
My theory was that the cable itself was stretched to the point of ineffectiveness. I ordered up a new one from BJ's and proceeded with the install. I chocked the tires, made sure it was in park, and then started the tear down. It was rather simple. I just need to disengage the parking brake itself and remove the cable end from where it meets up with the pedal.
In this photo, you can see the cable tucked up in the corner. The large black steel bar on the left is the foot-activated brake level arm. The cable mounts up to the end of the level arm like a giant bike brake cable, and a squared C-clip holds the sleeve in place. Pull it first to get a little slack, pop the C-clip, loosen the cable underneath the vehicle, and then slide the lead cylinder out of its pocket in the brake arm. It's now free to be pulled out from underneath the rig.
The sleeve and cable housing slides up between the inner and outer driver's side fender wells.
It then slides through holes in the frame rail and the transmission cross member where it meets up with the U cable that runs from one drum brake to the other.
My theory was that the cable itself was stretched to the point of ineffectiveness. I ordered up a new one from BJ's and proceeded with the install. I chocked the tires, made sure it was in park, and then started the tear down. It was rather simple. I just need to disengage the parking brake itself and remove the cable end from where it meets up with the pedal.
In this photo, you can see the cable tucked up in the corner. The large black steel bar on the left is the foot-activated brake level arm. The cable mounts up to the end of the level arm like a giant bike brake cable, and a squared C-clip holds the sleeve in place. Pull it first to get a little slack, pop the C-clip, loosen the cable underneath the vehicle, and then slide the lead cylinder out of its pocket in the brake arm. It's now free to be pulled out from underneath the rig.
The sleeve and cable housing slides up between the inner and outer driver's side fender wells.
It then slides through holes in the frame rail and the transmission cross member where it meets up with the U cable that runs from one drum brake to the other.
The threaded rod in the center of the pic below is at the end of the new brake cable, just under the rearward end of the front driveshaft. This is where the adjustment takes place. There's another on the passenger side. You control how much tension pre-load is on the rear drums. Not enough, and the e-brake doesn't fully engage and hold the vehicle in place. Too much, and the brakes are always slightly on as you drive. I figure it out entirely by trial and error. Note: use the double-nuts to lock your adjustment position in.
Thursday, August 18, 2011
Fuel hoses, part II
To my irritation, one of the return fuel lines was not hooked up when I picked up the rig from Hall's Engines in Moreno Valley. It was an easy fix. While I was in there, I replaced a few other rubber lines that looked old. I like fresh rubber, especially considering the wide variety of dry rot my 1973 VW Bug suffered from after sitting for a decade in the previous owner's garage. When my dad and I swapped vehicles so that I could take his Nissan pickup truck on my honeymoon (to haul my and Mrs.'s bikes up to Mammoth Lakes), the Bug's right rear tire blew out, even though it had plenty of tread left. The side wall shredded, scraping up the rear fender with all the exposed steel belting. Not good. Whenever I can, I replace old or suspect rubber with new, without question or second thought. It ain't worth the possible hassle given the minimal cost.
Monday, May 2, 2011
Finally got the Jeep back on Friday!
After ten months at Hall's Engine in Moreno Valley, I was able to pick it up. To my dissatisfaction, they were not, after all this time, able to get the transmission leak under control, so that's up to me to deal with later. But they did manage to get it to pass smog, the least they could do given that they rebuilt the engine.
In hindsight, I should have done things a bit differently, perhaps finding a different builder or a less expensive one. I get the feeling that after the rebuild was paid for, I was more an annoyance than a customer. So it goes. But we are moving in a few weeks to live at my parents' house in Carlsbad for a month before we can move into the new house in Yorba Linda, and now I got my Jeep back.
In hindsight, I should have done things a bit differently, perhaps finding a different builder or a less expensive one. I get the feeling that after the rebuild was paid for, I was more an annoyance than a customer. So it goes. But we are moving in a few weeks to live at my parents' house in Carlsbad for a month before we can move into the new house in Yorba Linda, and now I got my Jeep back.
Monday, May 31, 2010
Working on the tailgate
Like many FSJ owners, I had tailgate window issues. It would make a lovely popping/grinding noise whenever I put the window up. In order to get it into position, I consistently had to grab the top of the window and pull it up at least halfway while engaging the key in the tailgate. Not fun, of course. I started by dropping the window and the tailgate. I ordered a tailgate channel from BJ's last week so that when I dove in, I'd have the materials I needed.
The first step is to drop the tailgate and remove the carpet and the access panel. Just take out the fourteen screws holding the chrome metal strips in place on the carpet, and then take off the twelve that hold the access panel. Stay organized, however, because these screws are at specific lengths to avoid hitting anything of the internal workings of the tailgate itself. Here's what I found.

In the pic below, notice the two large gears with the 1 1/4" flatstock steel bars. As the motor rotates the driver's side gear, it moves the flat bars which are attached to the lifter channel via small bolts and a pair of spring-loaded washers.







I added little green grease, and now I'm done. After buttoning the tailgate back up, I had a fully compliant tailgate window. I think when I'm bored and in the mood for some quick little project, I'll open the tailgate back up and glue the plywood strips together and use some silicon adhesive to hold the plywood to the tailgate wall.
Sunday, May 23, 2010
Another run to El Mirage
Here are some videos of the kids behind the wheel at El Mirage OHV. Just click on a name to watch the video from my Photobucket account. They're each one or two minutes long but quite fun and funny. Pay particular attention to the background to get a sense of their turns and speed.

Friday, May 21, 2010
New exhaust system
When the engine was getting rebuilt at Hall's, Greg noticed that the catalytic converter wasn't heating up, which means it isn't functioning correctly. (A cat needs to get to at least 600 degrees to really work well in terms of emissions control, though they can run as hot as 1500 degrees without damage.) Unfortunately, excess heat can lead to other interesting side effects. Here's what I found when I peeked into my old converter.

Not exactly an effective set up. I'm kind of amazed that the thing passed emissions with this. How bad does one of these have to be to fail?
My new Magnaflow cat from BJ's is a great replacement for the original one. It's CARB legal, which is a requirement here in California. I know this thing is old and sucks gas, but I still want to have a clean running rig.

Since a converter change was necessary, I decided to go whole hog. Earlier this year, I'd noticed just how truly lousy the welds were at the joints of the exhaust system, including the AIR return tube from the cat back to the exhaust manifolds. Here's the 3"-to-2 1/2" neckdown transition from the Y-pipe to the cat. Ugly. I have a more elegant, or at least less messy, solution that I put into practice today on the other side of the cat, which I'll get to later. This one stays for now, however, because I will be having Hall's put on a pair of Doug Thorley headers with a 3" Y-pipe, which means this junk will be going bye-bye then.

Here's my muffler, which I've come to understand is not stock/OEM. This one is quite long (~30") and looks to be a no-name brand. For better or worse, from the cat back this thing was one big welded chunk, so I had to remove it first.



Because it's one chunk and I didn't feel like going to town on it with my Sawzall, I worked it forward, rotating the tailpipe over the rear axle and then pulling it out under the driver's side door. Easy. The cat also was simple to remove, again just an exhaust clamp holding it in place.









Swapped door locks


This morning I switched out the door locks from the driver's side and the passenger's side. The driver's side was in poor shape with the little parts where the key enters the mechanism moving around, so I pulled the retaining clips on both doors (in the far right pic), popped out the lock mechanisms, and traded them. The passenger side, since it isn't used much, was in quite good condition. While each was out, I put a little black silicon around the bezel to seal it up since the original plastic seals were shot. It was an easy fix.
Friday, May 14, 2010
Transmission pan leak and fix, round two
Didn't work with a cork gasket. I think the pan in the passenger rear corner is warped. I tried it again, draining and saving the freshly installed fluids. I added a rubber gasket plus some special Permatex RTV for transmissions. (NEVER use normal RTV on a transmission gasket because it will be dissolved by additives in the transmission oil.)
Still didn't work. I'll pull it again and hammer on the pan to try to true it up. We'll see.
For what it's worth, I'm not frustrated much by this. With the drain plug in place, it's much easier to repeatedly drop the pan as I try to get the leak fixed. I'm gettin' real good at it.
Monday, May 10, 2010
Transmission pan leak and fix
My transmission pan has been leaking way too much from the passenger side, especially since it's been sitting. Hall's offered to fix it, but I wanted to take care of it both to save the labor cost and to install a drain hole. Without a drain hole, here's how I normally have to get the oil out of the pan.

Not pretty. It just dumps out, and I hope the drain bucket catches it all. To affect change, I drilled a 1/2" hole with my nifty new drill press set to 600RPMs (slow and steady for drilling metal). It wasn't quite the right fit, so I widened it a bit. The way the drain hole adapter works is fairly simple. It's a large threaded bolt that goes through the drilled hole into the pan. A nut holds it in place, with a teflon washer on the outside for sealing. The inside of the large bolt is threaded as well, and a smaller bolt goes into that. Here's where I decided to put the hole:

This is a shot of it from the outside. Note the teflon washer. I located the hole in the front driver's side corner because I felt that area had the most clearance away from the transmission internals.

With the smaller bolt plug in place. In the upper right of the pic, note the front drive shaft.

It was a fun little project. I'd had the drain plug adapter for about a year in a box, so it was nice to finally be able to put it on.
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